
I bought the RR at a local auction yard, the classics are
practically extinct here in Manitoba, Canada. I had all but decided to
import a nice clean one from the U.S when this ratty specimen popped up
local. No one knew what it was so I got it for $3500 Cad. I accepted
that the lower cost to buy a "scruffy" unit would offset the tidy up
needed.
Once I had the Rangie I started to search all my usual haunts for a
"nice" diesel to fit in it. Having done an Isuzu swap while still
living in the U.K I naturally wanted to find an Isuzu. A new one in
Canada was a staggering $10,850. When I got up off the floor I quietly
backed out of the dealers and went in search of something more
affordable. All the engines I could find in North America are what I
call "clunkers"; slow speed industrials. After a disheartening search I
turned to ebay to see what I could find. On the second search I found a
brand new Isuzu 2.8l TD in Australia. This was the engine that Isuzu
was shipping to replace the disastrous 3L engine. Anyway, this bloke in
Australia had one to replace the blown 3L in his trooper but then sold
the trooper and got left with the engine hence it was being sold off.
It was the exact engine I wanted and I suspected it would sell high
going by the prices that they sold for in the Brit conversion kits. The
bid was ending late at night so I decided on a final price I could
afford factoring in shipping. I put a bid of $2200 USd on it and went
to bed. The next morning I was the proud owner of an Isuzu for $1750. I
couldn't believe my luck.
Photo at right:
The new engine arrives!
The Isuzu 4JB1 is a 2.8L diesel engine rated
at 120 Bhp.
It is very comparable with the original Range Rover Diesel models. The
Isuzu is used in the Isuzu Trooper and the Holden Rodeo so it is quite
matched to this size of vehicle. There is a sticker on the rocker cover
that states its was built to comply with the (Australian Design Rules)
ADR70/00 emmissions standards. It is very clean running.
While the engine was enroute from Oz to Canada I proceeded to remove
the gas guzzling lump of Aluminum that Rover calls an engine. I cleared
the engine bay completely, did my customary worship to the rust gods by
the light of a mig welder and prepped everything I could finishing with
a coat of red oxide rust primer. The engine arrived, despite the
best efforts of the Vancouver dock strike. The first few days all I
could do was look at it appreciatively, caress it a bit and when the
wife wasn't looking, left tongue prints on it. I have never owned a
brand spanking new diesel before. It was a thing of beauty. Typical
Japanese perfection. It was a complete drop in including alternator,
power steering pump, vac pump, engine mounts, wiring harness,
everything basically.
Measuring Up for Mating
the Diesel Engine to the Transmisison
Once I got over the initial excitement I set about the more
complex task of actually mating this to my ZF automatic. The initial
assessment showed that the thick standard flywheel on the Isuzu would
actually be a help because the torque converter is actually quite
recessed in the bell housing. The original engine has a spacer to move
the flex plate back a couple of inches to meet it. After a series of
measurements that determined the original flex plate depth into the
housing I believe I came up with the measurement of 1.230" deep. This
can shift a bit either way as there is some allowance in the design of
the torque converter. This allowed me to make a start on the adapter
plate which is the most complex component.
Photo at right:
Bare back end of new engine that has to be mated to the RR transmission
Machining the Adapter Plate
I measured the maximum radius of the bell housing an cut a circle of
plate from a scrap condenser housing that was laying in the yard. It
was 1.375" thick which gave me plenty of room. I set it up in the
lathe, faced off one side and bored a hole in the middle that fit the
end of the crank on the Isuzu. I then flipped it in the chuck and faced
the other side ensuring the faces were parallel and the center hole
running true. I faced off the second side down to the finished adapter
thickness mentioned above. I then bored half way through the plate to
the diameter of the old engines crankshaft end. I took this very
heavy slab of plate to the Isuzu engine from which I had removed the
flywheel, dowels and factory adapter plate to leave a flat block end
(see photo at right). I established a "horizontal" scribe line for
reference across the adapter and wiggled it onto the bare crank end.
Once it was securely clamped I started with the dowel holes. I
carefully drilled them out near size then reamed the holes to provide
and exact fit for a .500" dowel. With the dowels tapped in place I then
began the layout scribing of the starter position and holes, the bolt
circle and recesses needed to clear bolt heads etc. When I was
happy I had all the detail marked I removed the plate and went to the
old engine. This was a little more tricky as all he holes are blind. I
removed the dowels and machined two dowels with "center punch" points
that protruded a slight amount above the mating surface. The most
important fact here is to remember to offer up the same face of the
adapter as was marked on the Isuzu, not the blank side or it will be
ruined by the "mirror effect". I slid the adapter onto the end of the
crank, aligned the horizontal line to the Rover engine and gave it two
sharp whacks with a copper mallet over the dowels. This created two
nice center punch points which let me carefully drill and ream them in
the Milling machine. When I offered the adapter back up to the engine
the dowels fit with a light tap from the hammer.

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Raw material for the adapter
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Checking the fit of the placte
on the Rover engine |
The last stage was to get the bolt pattern from the rover which again
is all blind. I decided that supreme accuracy was not needed here so I
took the easy way out. I cleaned the mating surface and applied a nice
smear of machinists dye around each bolt hole, offered up the adapter
and with the dowels engaged I tapped it all over with a copper mallet.
When I removed the adapter it had some neat blue circles that I could
then carefully center and prick punch. With all the holes marked it was
then down to a few hours in the mill drilling clearance holes,
threading some holes and recessing the heads of those that would
interfere and generally avoiding cocking up the dowel holes that
required no further machining. A recess was milled for the Isuzu
starter and a cutout in the periphery of the adapter to receive the
transmission stay bar nut.
The final job was to chuck the whole plate back in the lathe and bore
the center out to clear the Isuzu flywheel (photo below).
Photo
showing the center of the adapter being bored out to final size
I am sure all this is a clear as mud but this is a very complex plate
to make. It took me about 16 hours. If someone is mad enough to try it
I will happily guide them through in greater detail!
Making a Flex Plate Adapter
The next step in the conversion was fitting the flex plate to a
standard clutch flywheel. Having already determined the "depth" that
the flex plate must protrude into the bell housing I used a series of
depth measurements to determine how much "gap" I had to fill between
the face of the flywheel and the back of the flex plate. I failed to
note this dimension down as I make most of the parts up in my head as I
go along. Basically I machined a recess in the face of the flywheel
with a ring of six bolt holes tapped into the flywheel .375 UNC. I then
machined a disc of .500" plate to fit the recess machined in the
flywheel. In the center of this disc I placed a centering hole that
mated to the existing spacer reused from the old rover engine. I
machined the Rover spacer to the appropriate thickness and fastened it
to the disc using the original 12 mm bolts. I hope that is fairly clear
as I cannot find a photo of that currently.
Fitting the New Engine into the Rover
With all this complete it was dangerously close to fitting the engine
into the rover. The only stumbling block was needing some 12 x 1.00
allen blots for the Isuzu. Once I had my hands on those it was all
systems go. One of the impracticalities of this project was that with a
solid flywheel there is no way to bolt the torque converter to the flex
plate after the engine is in place. This left me with the crappy option
of having to bolt the torque converter to the flex plate and install
the complete unit as one. This means an extremely delicate guiding of
the torque converter onto the two splines and drive dog of the trans
pump without nicking the seal. It was tricky but not the worst
thing I have ever done. I had put a new trans input seal in first to
get the best chance of success. The two drive splines entered well but
the pump was obviously rotating with the engine as i tried to "wiggle"
it in. After a frustrating 40 mins or so the was a sudden soft clunk
and everything fell together. I almost passed out with relief when I
realized the two dowels had also just slid in without the slightest
struggle !! The weird and wonderful center punch dowel scheme had
worked perfectly. Once I calmed down a bit I quickly put in a couple of
bell housing bolts before the whole lot could slid accidentally apart
again. Only time would tell if the seal had survived the ordeal.
Leveling the Engine and Adapting
the Engine Mounts
The next session involved leveling the engine in the bay. There is no
real high tech method to this.I personally marked the front cross
member where the center of the old crankshaft pulley used to be and
then lined the Isuzu pulley up to that. I also made sure that the
bonnet would clear which was only just. When I was happy with the
location of the engine I set about modifying the original Isuzu mounts
to fit the rover chassis. On the passenger side this involved making a
.500" thick adapter plate that bolted to the range rover then bolted to
the Isuzu mount. The Isuzu mounts where much wider and two bolt as
opposed to the Rover single bolt units. On the driver side I had to add
a small bracket to widen the rover mount as there was very little free
space. Pictures of the two mounts appear below.
With
the mounts complete I let the weight of the engine down and the rover
had a new heart. I probably took an hour or two out just fettling and
coveting. It was all down to the first start of the engine and see if
oil poured from the trans input seal!